dyno [B]PROOF[/B] on k&n filters....... part 2

stangman

15 Year Member
Jul 10, 2003
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dyno PROOF on k&n filters....... part 2

well here's the "proof" for you guys that were pitching a fit in my other thread. it's all in black in white, done on the same day, under the same circumstances, so believe it or not, here it is :D & by the way i can post dyno sheets if you like, but i will have to email them to someone else & have them post them :nice:

btw -- this was done on a mustang dyno, so pay attention to gains & losses & not the actual numbers. mustang dynos read lower than dynojets, so there is nothing wrong with my car.

please note .......car is in stock form aside from removed silencer :nice:

here were the weather conditions.......temperature -- 63 F
barometer -- 30.3 (104)
humidity -- 48%

run #1) WITH k&n -- 208.8 hp @ 5250
244.1 tq @ 4250

run #2) WITH k&n -- 210.7 hp @ 4750
244.1 tq @ 4250

run #3) STOCK -- 215.5 hp @ 4750
246.9 tq @ 4250

run #4) STOCK -- 217.6 hp @ 4750
247.9 tq @ 4250

Here are the averages...... WITH k&N -- 209.75 hp & 244.1 tq
W/O k&n -- 216.5 hp & 247.4 tq

There WAS a LOSS of .......6.6 hp & 3.3 tq


so with all of that out of the way..... if you don't believe it i could care less, it's there in black & white. don't get all pissed at me cause you possibly wasted 55 - 60 bucks just like me. also the reason i sad "possibly" is i will also do a test between the 2 air filters again next week, after my exhaust is installed, to see if the K&N gains power after my exhaust is much less restricted.
so if you don't believe this, i doubt i could convince you the sky is blue :rolleyes:


also....... ALL RUNS WERE DONE AT OPERATING TEMPERATURE, THERE WAS NO WARMING UP, or cooling down during the test, i put that in there because i noticed that the power just kept going up :D

so there you all go....enjoy :D
 
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oh yeah, one more thing..... when we took the k&n out for the last two runs we forgot to plug the mass air back in :nonono: :bang: , so there might have been more in there somwhere :shrug: i know it wouldn't make that much of a difference, since it doesn't do that much under wide open throttle. but every little bit helps. i didn't find out unitl i got off the dyno & "tried" to drive away :rlaugh: :bang:
 
98superstangGT said:
even if he didnt have that originally thats what he was saying he was going to do......im sure you read that one so you should have known.
I didn't read the last half of the other thread. The post-hoes started going crazy and I skipped it, and then it got locked. So I didn't know he was going to dyno again (hence my question above) and his original post made no mention of using the stock filter. Why not call those runs w/stock instead of w/o K&N? It would have been clear that way.

Anyhow, back on subject - those numbers are shocking if true. Since the power just kept going up, I wonder what two more runs at the end with the K&N back on would have produced?
 
02whtgt said:
Thanks for taking the time to do some research on this! :nice:

Will you email me the dyno slips? [email protected]


i'm on my way to work now, so i should be back around 10 p.m. or so & i will try to scan them & send them to you then, if i can't get my scanner to work (been having a little trouble with it) i will try & get boss281mustang to scan them for me :nice: see you all in a little while