Ok heres it went it down..
Had the car on the dyno, he burnt a quick chip, real conservative. He ran it up to 3k a couple times, it was making 360 rwtq at that point, exhaust was starting to get black as he got on it (rich), the air/fuel was at 10-1.
So everthing looked great at that point, he went ahead and ran it up to 5k, air/fuel was right at 10-1, still real rich, and boom, the upper rad hose goes flying the **** off, drenching us in antifreeze, luckily it was only at 135 degrees or so. He shut it down immediatly.
At first glance, we thought it was just the upper rad hose, so we threw a new clamp on there, leaving the rad cap off. He went to start the car, and the coolant shot out the rad about 3 feet. Blown HG!!
So wtf is going on here, we took out the 5 plugs that are easy to get too, and they all looked good, none ghost white like last time.
We really are at a loss to what the problem could be. I torqued the heads correctly both times. My thoughts so far are: 1) One bad injector? Would the air/fuel still be THAT rich though? 2) block warped somehow? 3) heads warped some how? 4) junk arp bolts?
Im kinda loosing my interest in boost now, two HG's in 1 week is crap. I figure ill give it ONE more shot with some of those ROL gaskets and see what happens. IF i pop another for no f'ing reason, im doing like vib and going with a fuelie 408.
Well im pretty pissed to say the least after the 240 towing bill lol. Thankfulling the dyno shop owner(mike dez) was nice enough to only charge me 100 even though we were there for 4 hours.
Any ideas guys?
Had the car on the dyno, he burnt a quick chip, real conservative. He ran it up to 3k a couple times, it was making 360 rwtq at that point, exhaust was starting to get black as he got on it (rich), the air/fuel was at 10-1.
So everthing looked great at that point, he went ahead and ran it up to 5k, air/fuel was right at 10-1, still real rich, and boom, the upper rad hose goes flying the **** off, drenching us in antifreeze, luckily it was only at 135 degrees or so. He shut it down immediatly.
At first glance, we thought it was just the upper rad hose, so we threw a new clamp on there, leaving the rad cap off. He went to start the car, and the coolant shot out the rad about 3 feet. Blown HG!!
So wtf is going on here, we took out the 5 plugs that are easy to get too, and they all looked good, none ghost white like last time.
We really are at a loss to what the problem could be. I torqued the heads correctly both times. My thoughts so far are: 1) One bad injector? Would the air/fuel still be THAT rich though? 2) block warped somehow? 3) heads warped some how? 4) junk arp bolts?
Im kinda loosing my interest in boost now, two HG's in 1 week is crap. I figure ill give it ONE more shot with some of those ROL gaskets and see what happens. IF i pop another for no f'ing reason, im doing like vib and going with a fuelie 408.
Well im pretty pissed to say the least after the 240 towing bill lol. Thankfulling the dyno shop owner(mike dez) was nice enough to only charge me 100 even though we were there for 4 hours.
Any ideas guys?