Something wrong??

Hey guys,

I just had my 347 installed and it is now running. The car does not move with anything more than 1/4 throttle, and nearly dies if i push the accelerator any further. My combo is as follows.....

347
AFR 165
Trick flow track heat
E cam
75mm tb.
75mm MAF
30lb inj.
255 pump
and all supporting mods
all new sensors..ect..

This car may not run the way it would when it is tuned, but i would think it would still run decent. There is also a shake at around 1500rpms. any help would be greatly appriciated,

Thanks,

Lenny
 
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I dont know how else to describe it. The car has NO power, and doesnt like to rev above 3k. it idles fine, oil is clean. doesnt burn oil. plugs are a light tan, seem to have some carbon on the rim of the plug. any other questions, i will be happy to awnser them. fuel pressure is at 42. Just Need HELP. All this money, and the car doesnt have the power to pass a vw beetle. :nonono:
 
Lenny

The tune is not gonna be real close with the stock pcm

but

It ought to be close enough to run better than that.

You most likely got something silly that is not as it should be.

Look for stuff like

wrong spark plugs
plug wires not right
big vaccum leak
exhaust restriction
fuel restriction
dizzy off time
bad coil
valves too tight

stuff kinda along those lines

just check EVERYTHING all over again and you'll find it.

Good Luck Lenny

Grady
 
Car seems to run really rich. checked wires, replaced wires. Nothing to restrict exhaust. took it off though, and checked it. clear. checked and replaced coil. autolite 3924s. triple checked order of wires. How do i go about checking if the valves are to tight? Also, a strange thing happened today. car remained running like *****, but stopped at the grocery store, and ran in. came out 5-10 min. later. got in the car. drove to the light. usually i push the throttle until it begins to bog down (a little less than 1/4 throttle.) and let off a touch. but the car didnt do it so i mashed on the gas and it got up and went through 1st, 2nd , and 3rd. Tried it again, and same result. What would cause this? any ideas guys. car has alost 500 miles on the motor. thanks for all the help.

Lenny
 
I suggest taking it back to the people who did the work. I wouldn't touch, remove or test anything. Also, the stuff you did do, I would not tell them you did it because they may try the finger pointing game. Take it back and have them test drive to repeat the condition while you are with them in the car of course.

Just curious. Why did you go with AFR 165 instead of the 185s?