Well here's another happy Edelbrock Performer/AFR 165's/FTI cam stanger
I was at the track yesterday. It was an OK weather. Not cold but at least no humidity like last time I went Since that last time, I had the Xenon bodykit removed, I changed my timing curve a little, I had that Raptor shiftlight put in (Thank God) and had the UPR triple hook quadrant and Extreme firewall adjuster(Thank God even more).
The only thing bad was that my rearend is pretty much shot. I've been hearing weird noises for like 10 days and I had my doubts. So yesterday, I was doing pretty much 1 wheel burnout The driver side isnt spinning. I GUARANTEE better times the next time I go, If I get my rearend fixed.
Beleive it or not, my home computer has broken yesterday morning. I'm at my grandmother's right now..So I cant scan my slips. I will though as soon as possible, beleive me
Here's my runs
12.9x@108
[email protected]
[email protected] (I bugged..tires gripped too much)
[email protected]
[email protected]
I didnt do not even 1 run in the 13's. Last time I went, I was trapping at 106mph. One more thing. On all the passes (I think but at least 4 of them), at least my driver wheel was off the ground to 3 inches high !! On N/A power. I'm suppose to have pictures of that and have plenty of witnesses All this on 100% STREET FORM, and UNTUNED.
The bad news now. Something happened to the car on the way back home..I was pretty much stopping to check my fuel pressure cause the A/F ratio gauge was saying I was lean. So I pulled over and then I heard that clapping weird noise that was coming under the passenger valve cover I noticed it was cracked on top. I had the stang towed. I opened it up today and I found 2 broken head studs and my rockers were loose in the valve cover . It seems that my pushrods and rockers are still intact and perfect. I dont think my head is damaged. Just those 2 studs. It was my fault.....one that last run, I kept the rev REALLY high somehow and I think I experienced valve-floating that resulted in this. Maybe I'm totally off but thats what I'm thinking. I'll have everything fixed this week.
At least my main goal is achieved. I'm so happy. Thanks ED !
I was at the track yesterday. It was an OK weather. Not cold but at least no humidity like last time I went Since that last time, I had the Xenon bodykit removed, I changed my timing curve a little, I had that Raptor shiftlight put in (Thank God) and had the UPR triple hook quadrant and Extreme firewall adjuster(Thank God even more).
The only thing bad was that my rearend is pretty much shot. I've been hearing weird noises for like 10 days and I had my doubts. So yesterday, I was doing pretty much 1 wheel burnout The driver side isnt spinning. I GUARANTEE better times the next time I go, If I get my rearend fixed.
Beleive it or not, my home computer has broken yesterday morning. I'm at my grandmother's right now..So I cant scan my slips. I will though as soon as possible, beleive me
Here's my runs
12.9x@108
[email protected]
[email protected] (I bugged..tires gripped too much)
[email protected]
[email protected]
I didnt do not even 1 run in the 13's. Last time I went, I was trapping at 106mph. One more thing. On all the passes (I think but at least 4 of them), at least my driver wheel was off the ground to 3 inches high !! On N/A power. I'm suppose to have pictures of that and have plenty of witnesses All this on 100% STREET FORM, and UNTUNED.
The bad news now. Something happened to the car on the way back home..I was pretty much stopping to check my fuel pressure cause the A/F ratio gauge was saying I was lean. So I pulled over and then I heard that clapping weird noise that was coming under the passenger valve cover I noticed it was cracked on top. I had the stang towed. I opened it up today and I found 2 broken head studs and my rockers were loose in the valve cover . It seems that my pushrods and rockers are still intact and perfect. I dont think my head is damaged. Just those 2 studs. It was my fault.....one that last run, I kept the rev REALLY high somehow and I think I experienced valve-floating that resulted in this. Maybe I'm totally off but thats what I'm thinking. I'll have everything fixed this week.
At least my main goal is achieved. I'm so happy. Thanks ED !