Well, the install is almost complete. It took a lot longer than expected because we ended up just pulling the motor. The passenger side header was a tight fit, and then we couldn't get the top three bolts started. We tried disconnecting the motor mounts, thought about dropping the k-member, but finally just said the best way is to pull the motor. Within four hours the motor was pulled, the new headers installed, changed the trans fluid, and reinstalled the motor, trans, and mid-pipe exhaust. All that is left do tommorow (I mean later today) is to add coolant and recharge the a/c system. We didn't fire it up yet because it was too late at night, but I will tell you guys how is sounds vs. my current setup. Sorry again for no pics, but I don't own a digi.
BTW a big thanks goes out to my buddy for helping me. This is definitely not a job for the weekend warrior. I have done some serious jobs in the past, and this one is up there for a major PITA. I don't have experience with other headers, but my buddy who helped me has done numerous on other mustangs (both long tubes and short tubes) and he said that he has never seen anything like this before. It must be
BBK's new tuned length design. But right now I would like to kick their designer's a$$ because I don't think there was any other possible way. Even with the motor out, some of the header bolts were still pretty hard to get to.